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Namco Volume Controller SLPH-00015 and 3.3V Arduinos support #11
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I don't have that one and no one has reported about it, so I can't say for sure, but if it uses the neGcon protocol, it should work. Interesting question about 3.3V boards. I think they will work but you might need a strong external pull-up (1k) on the DAT line. |
ok, i will give a try when i have some free time and all the components required and report back here. |
forgot to ask: do you have some time-sensitive code in the lib that won’t work correctly @ 8MHz? |
I don't think so but I have never tested the lib at 8 MHz. I'd suggest using the hardware SPI pins for improved reliability. |
Any news about this? |
still haven't received all the needed parts, i suggest to leave this issue opened until it is verified. |
Ok, no problem! Just make sure to report back :). |
UPDATE: just built the adapter with a diymore Arduino USB @ 3.3V: tested with a DS2 controller first and it IS working fine! Btw it is NOT working with the Namco Volume Controller, anything i could try? |
Enable debug and report what you get. |
EDIT2: after a few tries, with the Volume Controller now i get this in the serial monitor:
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Another try after re-checking the wires, now it stops here:
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Try to uncomment the DUMP_COMMS #define in PsxNewLib.h, I need more info. |
there you go: (If it does not make any sense i may still have some loose wire on my prototype build i need to fix again) |
It doesn't make much sense, but I cannot make a useful analysis if I cannot trust the data you provide. Please make sure your wiring is solid and that you have 1k pull-ups on all lines, then produce a log and I will analyze that. |
Just got a Volume Controller and I can confirm that it uses the same protocol as the neGcon and is supported by PsxNewLib. |
Hello, I am using this library in an atmega8 at 8mhz, everything works, but there is a problem, it seems that it takes time to read the values of the control, something like a delay, I press, and release the control and in the code it takes a few seconds to detect that I release or press, what can I change to improve the speed? I even removed the delay from the loop of the program, but it's still the same bad. |
is it supported?
white Jap version
green Eur version (i have one of these)
Reportedly it is using the Negcon analog protocol.
side question: will this sketch also work with an 3.3V Pro Micro board (instead of using a level shifter)?
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